Cowl Pin Fix and Alternator Maintenance
Added 5/8/2011
Updated 6/2012
I thought this might be something that will help out some
builders, so
I took some pics and want to get the information out.
First, a confession....I did something stupid long ago. When
doing a prop balance, I was tempted to leave the top cowl off
while
doing the run cycles, but decided to put it on each time.
But, I
didn't want to completely screw in all of the screws each time,
because
we'd be taking it right off again. The 2 horizontal front to
back
pins were in, and felt tight, so I figured for 2 minute runs it
would
be no big deal. I was wrong. Those pins can and do
move
forward, in seconds, when running the engine, if you don't have
pin
keepers installed. Lesson learned, fast forward 5 years and
725
horus...
On a recent flight I landed and noticed that one of the pins was
starting to creep forward through the keeper. The reason
this
happens is because as the pin vibrates inside the aluminum hinge
section that makes the keeper, it wears the keeper away.
Eventually I had enough loosness that the pin started to slide
forward. The keeper still caught it and just due to the
angle,
kept the pin from moving very far, but, it was time to react.
I created 2 brand new keepers, and this time I wanted to make them
never be a problem again. I've really liked using the pin
method
for attaching the cowl. It's quick, easy, and looks real
nice. But, the hard part for me was always grabbing the
stubby
pin end to pull the pin out. You can see some paint gone
around
that hole, because I had to always reach in with a needle-nose
pliers
and spin the pin so the bent end was out, and then grab it with
another
pliers and pull. What I thought now was that I could perhaps
take
care of this problem at the same time.
So, I created my new keepers, made sure the pins were bent
properly to
use the keepers, and put them in position, noting where the pin
aligned
rotationally to the keeper so that I could bond them
together. I
slid the pins forward a few inches, mixed up some JB Weld and,
pushed
the JB weld into the inside of the eyelit of the hinge section,
surrounding the pin. Once dry, it performed a few functions:
- Keeps the pin from vibrating inside the aluminum eyelit
- Keeps the pin from moving forward due to much tighter fit
- Allows me to just flip the tab up after unscrewing it, and
grab
the tab to pull the pin
2012
Update
After flying with
the JB welded tabs for a while, one of them broke off when
removing the pin. I gave up on the JB weld idea and
went to my plan B. I purchased some new pin material
to completely remake the pins, and some Stainless hinge from
McMaster Carr with the same size eyelits. After
cutting the pins to length, I used silver solder and flux to
solder the stainless tab to the stainless pin. It is
now very very secure..far more than JB weld. I would
recommend either doing tabs like this right from the
beginning, or buy the filler plugs and use completely
internal hidden pins with nice RV-10 cowl filler plugs like
Sean Strasburg's plane has. If I were doing it from scratch,
I'd do mine just like his.
So now it's far more secure than before. The only problem I
had
recently was that the pin pulled out the rear of the JB Weld on
one
pin. It's awful hard to get a good bond on a stainless pin
with
any adhesive. So what I may explore is either making a
keeper out
of stainless and then soldering it to the pin directly, or if
there is
any lower temperature solder that would work between aluminum and
stainless, I could try that. For now I've tried to secure it
using a loctite product to see if that holds better, but at least
I
shouldn't have much worry about the pin moving forward
anymore. I
went 725 hours with the old method, so I should be able to get far
more
time out of just about anything I try from here on. I would
advise any new builder to just fix it right away. There are
numerous people that have made some far more classy looking covers
that
screw in to hold that pin. I would love to have one of those
nice
arrowhead shaped shiny metal covers. Maybe one day I'll get
around to that.
Alternator Issue
Recently I went to tension the alternator belt again. I
replaced
the belt not too long ago, just because it was a good time for me
to do
so, not wanting to wait until it was worn at all. But, prior
to
that, I didn't really know how you could judge a belt being
properly
tightened. On cars, it's always been easy for me. On
the
plane, I don't feel satisfied not knowing the proper tension...I
hate
to just go by feel because you can be way off.
What I found not too long ago is this:
Put a torque wrench on the alternator nut, and if you're
tensioning a
3/8" belt, you hold the prop still and try to spin the alternator
nut
with a torque wrench. A new belt should spin at between
11-13ft.lbs. One that's used should be set to
7-9ft.lbs. This would give you a tension that should prevent
slip, and not be hard on the bearings.
Apparently in the past I was hard on them. I did have times
when,
especially in warm humid weather, I could get slippage and it
would
squeal on startup until I pulled the power back so it could sync
up and
then it would be OK. Then I'd tighten the belt up and it
would be
good for a year or so. But, I'm sure I over-tightened it in
trying to get the squeal gone. I'd simply mark the bolt position
on the
slider arm, and then tighten it by moving the bolt down the slider
a
bit and securing it...checking it with my finger by pushing on the
belt. Not precise enough. So, I paid the price and
felt
wobble in my shaft when moving the pulley, and sent the alternator
back
to Plane-Power to have it checked out and rebuilt. They said
that
I had a spun bearing, and I paid for them to send me a brand-new
rebuild...using at least one of my old parts so it would qualify
as a
rebuild using the same s/n. The price was great, the service
and
turn-around was same-day, and I've now got a basically brand new
alternator mounted up. If nothing else, I learned valuable
lessons in belt tightening, and I can fly my next stretch of IFR
flight
secure in the knowledge that my alternator was brand new at 725
hours.